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Abstract:
Based on the shaking table test, the seismic response of the main parameters of the two span skew bridge was gutted. The finite element model of the test model was established by the finite element analysis software OpenSEES. An improved model of single beam quality distribution was proposed by employing the main beam model analysis and the support model analysis. Three direction ground motion input analysis was carried out to improve the quality distribution model of the single beam, and the seismic response of the structure under the three direction ground motion input was obtained. The comparison was made between the analytical results and experimental results. The results show that the improved single beam quality distribution model can consider the torsion effect of the beam and can greatly improve the efficiency of the calculation, and the analysis result is greatly improved, which is more close to the experimental data. © 2017, Editorial Department of Journal of Wuhan University of Technology. All right reserved.
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Journal of Wuhan University of Technology (Transportation Science and Engineering)
ISSN: 2095-3844
Year: 2017
Issue: 5
Volume: 41
Page: 751-756
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ESI Highly Cited Papers on the List: 0 Unfold All
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30 Days PV: 0
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